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Home > About Toshiba > Social and Environmental Activities > Environmental Management > Greening of Process > Mitigation of Climate Change: Energy-Derived CO₂


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Energy-Derived CO₂

Reducing energy-derived CO2 emissions

Energy-derived CO2 emissions for Toshiba Group are increasing as its business expands. In the future, the Group plans to build new plants mainly in semiconductor and new rechargeable battery operations in order to meet a lively demand in the market, and energy- derived CO2 emissions are expected to grow in the immediate future. In order to reduce total energy-derived CO2 emissions as much as possible and improve the overall CO2 emissions per unit production, Toshiba Group is introducing energy-saving processes and equipment with the aim of reducing energy-derived CO2 emissions by 45% compared to the 1990 level by FY2010 and by 47% compared to the 1990 level by FY2012. As a result, in FY2010, the Group reduced energy-derived CO2 emissions by 48%, achieving the goals. We will continue to actively promote capital investments such as using high-efficiency chillers and air-conditioning systems as well as introducing high-efficiency lighting system. In FY2011, CO2 emissions are expected to increase as a result of the Great East Japan Earthquake; however, Toshiba Group will actively incorporate energy-saving measures into its activities.

Energy-derived CO2 emissions

chart of Changes in energy-derived CO₂ emissions and per unit production

*
The CO2 emission coefficient for electricity on the user is used to calculate energy-derived CO2 emissions (3.50 t-CO2/10,000 kWh in FY2010). Overseas electricity is based on GHG Protocol.

Breakdown of energy-derived CO2 emissions in FY2010

graph of Breakdown of energy-derived CO₂ emissions in FY2010

Case Study: Reduction in CO2 emissions by shifting energy use / CET Toshiba (Changzhou) Transformer Co., Ltd.

photo of natural gas boilers

Changzhou Toshiba Transformer replaced coal-burning boilers with natural gas boilers in partnership with the Chinese city of Changzhou to improve air quality and promote a shift in industrial structure. By doing so, the company reduced annual CO2 emissions in 2010 by 7,114 tons (down approximately 65% compared to the previous year).

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Toshiba Corp.'s Fuchu Complex has reduced CO2 emissions by 400 tons annually in its laboratory, which introduced a photovoltaic power generation system and the latest energy-saving equipment.

photo of Building No. 11 (Laboratory) at Toshiba Corp.'s Fuchu Complex
Building No. 11 (Laboratory) at Toshiba Corp.'s Fuchu Complex

Establishing a new photovoltaic power generation laboratory with the latest energy-saving equipment

The new laboratory at Toshiba Corp.'s Fuchu Complex, which was established with the latest energy-saving equipment in November 2010, is conducting experiments on next-generation electricity networks.

1. Introduction of a photovoltaic power generation system

The Fuchu Complex introduced a photovoltaic power generation system capable of generating 398 kW of electricity. By combining SCiB™ secondary batteries with this system to control fluctuations in system output more effectively, the Complex successfully reduced CO2 emissions by 124 tons annually.

figure of photovoltaic power generation system

2. Making heat source equipment more efficient

The multi air conditioning system reduces CO2 emissions by 37 tons annually by introducing high-efficiency air conditioning and realizing optimal operation using Neuro-PMV™ Control and Building Energy Management System (BEMS).

figure of Making heat source equipment more efficient

3. Introduction of LED lighting and lighting control systems

E-CORE™ LED lamps are used for the office area and outdoor lights. In addition, a system, which enables optimal lighting control by combining motion sensors, automatic dimmers, and other devices, is installed in the work area. These measures help reduce 112 t-CO2 annually.

photo of Introduction of LED lighting and lighting control systems

4. Controlling CO2 emissions in the amount of ventilation

By using an inverter to control the amount of air taken in from the outside according to the concentration of CO2 in the room, reducing the energy used by heat sources, and cutting back on the power used to convey outside air, the Complex reduced CO2 emissions by 155 tons annually.

Controlling CO₂ emissions in the amount of ventilation

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Case Study in FY2008

Case Study: Energy conservation at a semiconductor factory / Oita Operations, Toshiba Corp.

photo of High-efficiency inverter refrigerator
High-efficiency inverter refrigerator

Clean rooms at semiconductor factories consume a large amount of energy for air-conditioning throughout the year. The Oita Operations substantially improved the overall efficiency of air-conditioning mainly by increasing the efficiency of refrigeration equipment and supplementary machine systems and establishing energy-saving automatic control systems. Through these measures, the factory reduced annual CO2 emissions by 12,291 tons.

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Case Studies in FY2007

Case Study 1: Energy Saving by Reduction of the Clean Room Air Circulation Flow / Oita Operations, Toshiba Corp.

Clean rooms at semiconductor factories consume a large amount of energy for air-conditioning throughout the year. The Oita Operations substantially improved the overall efficiency of air-conditioning mainly by increasing the efficiency of refrigeration equipment and supplementary machine systems and establishing energy-saving automatic control systems. Through these measures, the factory reduced annual CO2 emissions by 12,291 tons.

figure of The Clean Room Air Circulation Flow

Case Study 2: Energy Conservation at the TV Production Base in China / Toshiba Dalian Television Corporation

At Toshiba Dalian Television Corporation, which is Toshiba's TV production base in China, CO2 emissions decreased by 88% owing to the air conditioning of the newly introduced production line, via an intake of cold open air into the intra-room air conditioning for the heat application line during wintertime.

figure of The air conditioning of the newly introduced production line

Case Study 3: Energy-saving Semiconductor Manufacturing Plant / Oita Operations, Toshiba Corporation

At Toshiba Dalian Television Corporation, which is Toshiba's TV production base in China, CO2 emissions decreased by 88% owing to the air conditioning of the newly introduced production line, via an intake of cold open air into the intra-room air conditioning for the heat application line during wintertime.

photo of Hiroyuki Goto, Koji Gohyakuji, Yujiro Sakai, and Shinji Goto
(l to r) Hiroyuki Goto, Koji Gohyakuji, Yujiro Sakai, and Shinji Goto Facilities Management Group, Facilities Management Department, Oita Operations, Toshiba Corporation

photo of Clean Room
Clean Room

Improvement Measures and Effect

Improvement measure energy saved (t-CO2 ) Effect (million yen)
Reduction of steam consumption owing to the change of the humidifying method 1,545 36.3
Energy saving of pure water equipment (greater recovery of waste heat from the refrigerator) 447 9.8
Energy saving of pure water equipment (recovery of waste heat from the manufacturing equipment) 326 6.7
Total 2,348 52.8

Case Study 4: Energy Saving by the Introduction of Dryers with No Purge Loss

photo of Energy Saving by the Introduction of Dryers with No Purge Loss

AFPD Pte., Ltd., a Singapore-based subsidiary manufacturing low-temperature polysilicon TFT LCD cells, introduced dryers with no purge loss in fiscal 2006. As a result, the company reduced the amount of energy used to produce high-pressure dry air used in the manufacturing process.

Previously, adsorption-type heatless dryers were used for production of high-pressure dry air. However, 16% of the high-pressure dry air produced was used for treating the adsorbent. Thanks to the introduction of dryers with no purge loss that use reduced pressure for treating the adsorbent, high-pressure dry air is no longer used for that purpose. Measures implemented to enhance the overall efficiency of the high-pressure dry air production system have led to a 19% reduction in energy consumption. This translates into a 1,460t-CO2 reduction in CO2 emissions a year.

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